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A Pilot With A
Sordid Past, Authorities Arrest Missing Drug Pilot Barrington Slack By Eddy Metcalf |
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November 29, 2011 - On Monday at about 4 PM, Waller County
Sheriff’s Office Deputies and Department of Homeland
Security Agents arrested Barrington Carl Slack as he was
leaving from Carinos Italian Restaurant, East Humble,
Texas. Slack, 33, was identified as the pilot of the twin
engine aircraft that
crashed landed at the Houston Executive Airport in
Waller County on November 21, in which authorities could
not locate the pilot of an aircraft that was filled with
marijuana.
We
now have learned Slack has a sordid past. Back on
October 21, 2010, Slack departed Covington Municipal
Airport in a Rockwell International 112TC aircraft,
N1154J as pilot that he owned under the company name, Kalunji Aviation Group LLC. He climbed up to altitude,
put on his parachute and jumped out of the aircraft. The
Rockwell International crashed landed near Waynesboro,
Georgia.
Slack reported to the FAA he had picked up the airplane on this day after some maintenance work had been done on the plane and he was going to fly it back L.B. Owens Airport in Richland County, South Carolina. |
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Slack said
the airplane tanks were topped off, completed a preflight,
engine run-up, and did his pre-takeoff checklist prior to
takeoff. There were no anomalies. Slack performed 3 touch-and-go
landings at Covington Municipal Airport before departing for
L.B. Owens Airport.
Once en
route, Slack noticed that the elevator control was "stiff" as he
completed an altitude change. Then, the yoke would no longer
move fore and aft, and he then realized that he had lost elevator
control of the aircraft. Slack further stated that he had
aileron control and could turn left and right, but altitude
changes could only be made by increasing or decreasing engine
power. Eventually, he lost aileron control, and could only
perform shallow turns with rudder inputs.
Slack
declared an emergency over the radio to air traffic control
(ATC), and was provided with radar vectors to Augusta Regional
Airport (AGS), Augusta, Georgia. He attempted to troubleshoot
the problem over the radio with ATC and other pilots on his
assigned frequency, and then "started putting on a parachute I
had on board."
The pilot
made multiple approaches but could not complete the landing
before he began to run out of daylight, and his fuel state
became critical. He maneuvered the airplane south of the airport
towards a wooded area "away from homes." About 1,500 feet above
ground level, the airplane's fuel supply was exhausted, the
engine stopped producing power, and the pilot parachuted from
the airplane.
Slack
reported that in July 2010, “almost the complete instrument
panel” had been stolen from his airplane. A statement from the
pilot/owner’s insurance company revealed that the pilot was
compensated for the loss of his instruments. |
An examination of
the wreckage was performed at the crash site by FAA aviation safety
inspectors. All major components were accounted for at the scene, and no
evidence of pre-accident mechanical anomalies was noted.
There was a
significant amount of impact crushing of the cockpit that prevented
investigators from manipulating the cockpit controls “as found.” The
cockpit was cut and pried apart to gain access. All elevator cables were
connected to the elevator arms on the control yoke. The upper elevator
arm was bent about 45 degrees. The lower arm was undamaged. The control
yoke was then removed by cutting it in half. The left control yoke
cross-tube was fractured at the weld point on the control yoke column
due to impact and overstress.
The empennage was
cut from the aft fuselage during recovery of the wreckage. While impact
damage was evident, the elevator and rudder remained attached. The
elevator cables were also cut during wreckage recovery but remained
attached to the elevator bellcrank and the connections were in good
condition. The pushrod from the elevator bellcrank to the elevator horn
was attached and was in good condition. The horn and bellcrank moved
freely with no binding evident.
The elevator trim
actuators were examined, and each actuator was connected to its
respective trim tab. The trim tabs were found in the full tab down
positions. The chain drive was actuated manually and the chain moved
from stop-to-stop freely and showed no evidence of a lack of
lubrication. In summary, the examination of the empennage revealed no
evidence of any binding or restriction of movement of the elevator or
elevator trim surfaces.
Examination of the
instruments mounted in the instrument panel revealed that the serial
numbers on the air pressure instruments matched the serial numbers of
the air pressure instruments that were installed in the airplane when it
was purchased by the pilot/owner, and later reported stolen in July,
2010.
Slack exited the
airplane wearing a Softie emergency parachute. The pilot was asked how
it was that a parachute was on board, why he purchased one, and where
his training was obtained. When asked if he was a military parachutist,
he said no, but stated that he had served in the United States Marines
as an infantryman. He said that he had previously owned an L39 jet
trainer manufactured in the former Czechoslovakia. The pilot said he
sold the jet, but bought the parachute so that he could get instruction
in the jet from its current owner, as the ejection seats in the jet were
disabled. |
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